This is the second project on MPU6050 based 3-axis gyroscope. For wireless communication we use 433 Mhz RF. We had to face issues with transmitting data since the module is very low cost it generates noise. So, we had to design special noise filter for getting our job done.
Here is the video of our testing and final outcome.
Video and editing credit goes to Sayantan Roy Arko. Arko is one of my student from second batch. He has keen interest on robotics. He is really good at mechanical designing. He designed the beautiful body of the robot using PVC board.